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AT A TIME when fuel prices have skyrocketed
and companies across the board are doing their part to
be greener, a team of individuals from CSX Corp. came
together to reduce the large amount of fuel wasted
while locomotives sat idling.
The locomotive shutdown team used a variety of
quality tools and methods and ultimately came up with
a solution to increase shutdown time and decrease the
temperature at which locomotives could be shut down.
The project saved millions of dollars in the form of mil-
lions of gallons of diesel fuel.
In 50 Words Or Less • A team from the rail
company CSX Corp. found idling locomotives wasted 30 million gallons of diesel per year.
• Team members used quality tools, such as Six Sigma and FMEA, to reveal root causes and develop fuel conserving solutions.
• The result: a savings of more than $28 million over three years.
May 2008 • QP 21
TEAMS
It All Ties Together
fuel consumption,
It All Ties Together CSX team’s project curtails fuel consumption, saves company millions
by Nicole Adrian, contributing editor
QP • www.qualityprogress.com22
The team’s work earned it a bronze medal at the 2007
International Team Excellence Competition, sponsored
by ASQ’s Team and Workplace Excellence Forum. The
team presentations are judged annually at ASQ’s World
Conference on Quality and Improvement.
War on waste CSX locomotives were typically left idling when not in
use, even for relatively short periods of time. Idling lo-
comotives wasted four gallons of fuel per hour. But if
the shutdown occurred for too long a period, gaskets
would dry out, causing engine leaks.
In 2004, the locomotive shutdown project was cre-
ated out of a CSX Six Sigma process improvement
team (PIT+) that focused on fuel. PIT+ teams created
at this time were to look at all business processes and
major cost areas. The project arose out of organiza-
tional needs, using a top-down approach that focused
on waste elimination based on data and broad stake-
holder involvement.
Fuel made up nearly 10% of total operating expens-
es, and fuel prices were expected to increase in the
coming years. The fuel PIT+ developed a value driver
tree to focus in on high impact areas that could be rap-
idly implemented.
To fi gure out if a fuel conservation project was
worth attacking, the team tapped into data that was
used for exception reporting on locomotive dwell
times (see Figure 1). The median time a locomotive
didn’t move was 12 hours on a weekday and 14 to 16
hours on the weekend. About 3,600 locomotives were
in transit at any given time.
The team found that the idling locomotives wasted
30 million gallons per year. Armed with these num-
bers and data, the team decided the project was worth
tackling.
Getting involved Potential stakeholders in the locomotive shutdown
project participated in the effort to defi ne and launch
the project, each bringing valuable perspectives, in-
sights and concerns. The team validated the project
stakeholder perspective by using suppliers, inputs,
process step, outputs and customers (SIPOC), and in-
cluded the suppliers and customers as stakeholders.
Ultimately, the project involved stakeholders
across various work areas (see Table 1). This included
employees and people from:
• The senior leadership team (SLT).
• Locomotive management and shop.
• Transportation management, and train and engine
departments.
• Finance and purchasing.
• Environmental group.
• Communities served.
In the beginning, the SLT and
project champion addressed re-
sistance, allocated resources and
ensured project goals cascaded
through the organization. The fi -
nance and purchasing stakehold-
ers tracked and validated savings,
ensuring that budgeting activity re-
fl ected the project’s success. Tying
in the budget process further com-
mitted functional departments to
the project.
Employees who managed and
worked in locomotive shops and ser-
vice centers agreed with the project’s
aim but had concerns. Employees
reasoned that if the locomotives did
not restart easily and needed as-
sistance, it could hurt their facility
throughput and pull resources away
Reasons this project was selected / FIGURE 1
Fuel cost is a function of these key drivers: volume, productivity, engine idling, price and logistics costs.
Total fuel costs
Gallons
Cost/gallon
Base price/gallon (including taxes)
Distribution cost/gallon
Nonproductive use (sitting)
Productive use (pulling freight)
Gallons/hour Engine idle efficiency
Largely exogenous, reflects purchasing, tax efficiency and physical facility locations
Gallons/KGTM Diesel engine productivity
KGTM Measure of volume
Idle Time Waste = 30 million gallons (~6% of total usage)
(KGTM = thousand gross ton miles)
May 2008 • QP 23
from their primary tasks.
The transportation management and train and en-
gine employees also had concerns. These included:
• Yard delays caused by restarting locomotives.
• Initial start-up taking more time than it would have
with idling locomotive waiting.
• Locomotives shut down for a short period of time.
• Lack of locomotive maintenance assistance at out-
lying areas.
• A lapse in production.
• Poor service to customers.
To be successful, the team needed to maintain and
leverage the support of the SLT while increasing sup-
port from the locomotive shop and service center
employees, and the train and engine personnel. The
team also needed them to change their behavior. To
understand the degree of impact the project would
have on stakeholders and the reasons behind potential
resistance, the team used failure mode effects analysis
(FMEA).
The environmental group was an obvious project
supporter. The group envisioned fewer noise and
air pollution complaints from the communities CSX
serves. The environmental group had received com-
plaints from residents, who said the idling locomotives
disturbed their sleep. The residents also had concerns
about diesel fumes. The group also saw the opportu-
nity to gain emission reduction credits.
Choosing the mission To select the project, the team used familiar tools: Six
Sigma and defi ne, measure, analyze, improve and con-
trol (DMAIC).
Project selection also included some consider-
ations and measures:
• Data availability and quality.
• Projected benefi ts and savings.
• Impact on internal and external customers.
• Impact on existing initiatives.
• Locomotive idle time in hours.
• Gallons per hour consumed while idling.
• Historical total idle time.
The team used various tools to assess the type of
impact the project could have on stakeholders and all
units involved. These tools included:
• Subject matter expert (SME) input.
• FMEA.
• Change acceleration process tools.
TEAMS
Stakeholder involvement / TABLE 1
Stakeholder roles, involvement and impact of contribution to root cause analysis
Who: Role: Responsibility: Impact:
SLT and Champion Secure resources. Monthly champion reviews and oversight. Low
Locomotive management Locomotive Engineering support. Validate improper shutdowns. High and shop employees Transportation manage- Advise on issues perceived by Evaluate failures. High ment and T&E employees end users. Identify exceptions for missed opportunities.
Finance and purchasing Finance/budget analysis. Not process owners. Medium Provide cost per gallon.
Environment/ Help identify “other”occasions Support through idea generation. Low communities served of shutdown opportunity.
Black Belt support Data analysis. Perception on process variation. High Effectiveness of current controls.
Levels of Impact: Low = support role Medium = validation High = SMEs
QP • www.qualityprogress.com24
• Driver trees.
• Analytical tools.
The team found that 78% of the locomotive fl eet is
equipped with a global positioning system (GPS), which
generates an automated transmission each hour, provid-
ing information about the status of the locomotive and
whether it has moved since the last transmission.
To gauge the shutdown performance and to measure
the project’s impact and value, team members used infor-
mation about the locomotive’s identifi cation, latitude and
longitude of reporting, hours since last movement and if
the locomotive was running or shut down.
SMEs provided insights into the potential root causes
that stemmed from the FMEA. These ideas included:
• Employee knowledge and attitude.
• Current and expected ambient temperature.
• Dwell or sitting time of locomotive.
• Actionable opportunities.
• Applicable rules regarding when to shut down.
• Health of locomotive.
A questionnaire was then sent to all engineers to serve
as a fuel shutdown reminder and affi rmation, and to gain
their feedback and ideas. For the project to succeed, it
had to affect the behavior of more than 8,000 employees
in hundreds of locations throughout the eastern half of
the country.
Root cause analysis The team again used FMEA to identify issues of critical
importance to the stakeholders and to view the issues in
context with all stakeholder involvement. Additionally,
the team worked through a cause and effect matrix to
validate the insights from FMEA, relate the inputs to cus-
tomer requirements and prioritize potential root causes.
While team members developed SME insights from cause
and effect diagrams and FMEA, they also investigated
hard data, the GPS data from the locomotive fl eet and
other sources to confi rm SME insights.
The identifi cation and analysis of root causes started
with subjective insights followed by data collection and
analysis. The facts led to team agreement. The process in-
volved a wide variety of tools based on the type of infor-
mation and data available, which also created a common
perspective and commitment within the team.
These tools included:
• Process maps.
• FMEA.
• Cause and effect diagrams.
AN INSIDER’S VIEW I’ve worked for CSX Corp. for 34 years, and my father
and brother worked on the railroad. Railroading is in
my blood, and I know this industry very well. I realize
because of its 180-year history, there is a lot of tradi-
tion that can sometimes mean slow-moving processes
and resistance to change.
This changed at CSX when the company got in-
volved with Six Sigma and ASQ. From the start, I could
easily see how the Six Sigma process tore down the
walls that prevented our growth. Being involved with
the locomotive shutdown project is a perfect example
of how this process works at CSX and how it made me
see that we were changing for the better.
As one of the 32 fi nalists, our team was fi lled with
pride. To be included with some of the world’s cor-
porate leaders—companies such as Boeing, Siemens
and Genentech—was mind-boggling. This was the fi rst
time CSX was in the fi nals. When we marched into the
meeting with the other fi nalists, and as the streamers
were fl ying and the cheering crowd was using noise-
makers, it was hard to contain our excitement.
I remember that when it was announced that our
team was the bronze winner, we launched from our
seats and ran onto the stage, leaping and screaming
with excitement. I think my teammates would agree
that we didn’t feel this excitement just for ourselves.
We were accepting this coveted award for the entire
CSX Corp., and the employees who embraced this new
way of working. After generations of doing things the
same way, this was quite an amazing accomplishment.
Railroaders are full of a sense of pride in their work
because for nearly two centuries we’ve run trains.
Now, with this sort of process improvement, we don’t
just run trains—we run them well. This is the sort of
forward thinking that future generations of railroaders
will use to ensure that, indeed, CSX is how tomorrow
moves. — Dennis Merrell, core team member
After generations of doing things the same way, this was quite an amazing accomplishment. Rail- roaders are full of a sense of pride in their work because for nearly two centuries we’ve run trains.
“
”
May 2008 • QP 25
• Questionnaire/survey.
• Measurement system analysis.
• Statistical tests.
• Team agreement on results.
Following the rules The team found that locomotives were often left idling
because operators were simply following the compa-
ny’s rules. Before this project began, the CSX trans-
portation fuel conversation rule was to shut down die-
sel locomotive engines when they were not being used
for at least 30 minutes, and the ambient temperature
was above 40° F.
To develop possible solutions, the team benchmarked
other railroad shutdown practices—including those of
Burlington North Santa Fe Corp. and Canadian Nation-
al—to determine what risk levels railroad operators ac-
cepted. They discovered these other railroads supported
lower temperatures and time thresholds.
The team’s solution tree identifi ed several factors
that had statistical signifi cance to shutdown perfor-
mance—most were constrained by the fuel conserva-
tion rule. The data showed clear differences in per-
formance by location. It was also clear that shutdown
performance was impacted by temperature. Regres-
sion results on a fi tted line plot gave the team clues
that individuals had different interpretations of the
temperature.
A fi nal solution The team considered changing the
rule’s time and temperature limits,
which would result in increased em-
ployee awareness, rule adherence and
standardization of the delivery system
of temperature information. The team
used an improved FMEA to gauge the
solution’s potential value.
To understand the risk of increasing
shutdown opportunities by adjusting
the parameters of the rule, the team col-
lected data from temperature gages in-
stalled in the water system on a sample
of units in colder weather. Each of the
units had a dump valve installed so the
engine cooling water would automati-
cally drain when it reached 40° F, pre-
venting any possible freeze damage.
These samples indicated:
• At 28° F ambient temperature, it should take 32
hours for water temperature to reach 40° F.
• At 28° F ambient temperature, it should take 52
hours for the water temperature to reach freezing.
However, each locomotive had a different heat
transfer rate—the data on two of the units indicated
the water would reach 40° F in as little as 14 hours
TEAMS
TEAM MEMBERS WHO represented the CSX group at the 2007 International Team Competition were (from left) Andy John, Herb Schubert, Wayne Sequin, Dean Mene- fee, John Murphy and Dennis Merrell.
Final solution validation / FIGURE 2
Final solution opportunities
Cumulative % of locomotive idle time by temperature
35º - 30.44% 28º - 19.91%
32º - 24.80%
40º - 37.63%
100%
90%
80%
70%
60%
50%
40%
30%
20%
10%
0%
-3 1º
-2 0º
-1 3º -5 º 3º 10 º
17 º
23 º
29 º
35 º
42 º
48 º
55 º
62 º
69 º
77 º
84 º
Outside temperature at start of not-moving period
% o
f t ot
al n
ot m
ov in
g tim
e at
or b
el ow
t hi
s te
m pe
ra tu
re
3,800 locomotives subject to temperature variation
QP • www.qualityprogress.com26
and begin freezing at 25 hours. The data showed that
CSX can tolerate risk at 35° F for shutdown without
unusual risk of locomotive engine and components
damage. At 35° F ambient temperature, locomotive
cooling water will never reach freezing.
After analyzing the data, the team concluded it
would support two rule changes (see Figure 2, p. 25).
First, at selected locomotive shops and service centers
that were manned 24/7, the shutdown temperature
threshold would be decreased from 40° to 28° F. Sec-
ond, the temperature in the rule would be decreased
from 40° to 35° F, and the time would be decreased
from 30 minutes to 15. These changes were based on
benchmarking and validated by temperature decay re-
gressions. The rules were applied in September 2004.
Making changes After the rules were put into practice, large, obvi-
ous signs were built at locomotive shops to reinforce
when to shut down locomotives and when to leave
them running. Daily scorecards for each location and
division were and continue to be used to provide re-
sponsible fi eld offi cers with current, relevant and ac-
tionable data.
Each 1% change in shutdown performance gener-
ates more than a half million gallons of fuel annually,
The team found idling locomotives wasted 30 million gallons of fuel per year.
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May 2008 • QP 27
TEAMS
equaling more than $1 million in savings for each per-
centage point.
Some of the tangible and intangible results realized
include:
• Improvements to shutdown performance numbers
without collateral damage for operations’ mechani-
cal and transportation management.
• A savings of $3.6 million in 2004.
• Additional savings at specifi c shop locations.
• Train origins that were not impacted.
• Improved fuel effi ciency at a time when fuel costs
were escalating.
• An invitation to join the Environmental Protection
Agency’s greenhouse gas initiative.
• A savings of more than 14 million gallons of fuel and
more than $28 million over the three-year span of
the project.
• Better stewardship with regard to the environment
resources by reducing emissions and noise, which
has led to happier neighbors and recognition for the
achievements.
• A savings of more than 650,000 barrels of a non-
renewable fuel resource.
Beyond these results for CSX, the locomotive shut-
down team had results of its own. Over the course
of the project, the team members increased their fa-
miliarity and understanding of process improvement
tools and the workforce developed more disciplined
behavior. Several key members were identifi ed for per-
formance and received awards.
READ MORE TEAM COMPETITION ARTICLES Look for case studies on other winning projects from the 2007 International Team Competition on www.qualityprogress.com.